I figured it was just me getting used to the power of the WR3 setup since I've had it installed now for over 8 months....
I haven't logged a run in quite a while as it has been running well and I don't feel like messing with it but yesterday on my way home the DIC showed only 23psi and for the past several months, I've been running 26.5psi which pegs the DIC at 25.
Hooked up the VCM scanner for the trip to work this morning and confirmed that I am maxing out at 23.4psi so I ran the boost leak test and immediately found the culprit. The threaded hole to the left of the 3 bar sensor.
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I don't remember if I installed a fastener in this threaded hole or not when I installed the upgraded charge tubes and 3 bar sensors but it was the source of the leak. I installed a 10-32 x 1/2" screw with blue loctite in it and tested the system to 30psi with no leak now so I'll run a log on the way home to make sure I'm back to my tuned 26.5psi.
Just thought I'd post this as a heads up. There is no hole in the CAC pipe under the threaded hole here so the pressure must be weeping under the boss from the 3 bar sensor or the meth injector switch.